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Keywords: density ratio
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Proceedings Papers
Proc. ASME. GT2022, Volume 6A: Heat Transfer — Combustors; Film Cooling, V06AT12A020, June 13–17, 2022
Paper No: GT2022-82118
... by PSP technology. The effects of TBC on twisted vanes film cooling effectiveness were studied, which was sprayed by electron beam physical vapor deposition (EB-PVD). Three typical density ratio (DR) of 1.0, 1.5 and 2.0 and three mass flow ratio (MFR) of 8.92%,10.45% and 12.21% were test. The air...
Proceedings Papers
Proc. ASME. GT2021, Volume 5A: Heat Transfer — Combustors; Film Cooling, V05AT12A015, June 7–11, 2021
Paper No: GT2021-59366
... ratio (DR) effects are studied by testing at blowing ratios of 0.5, 1.0, and 1.5 and three density ratios of 1.0, 1.5, and 2.0. Three different foreign gases are used to create density ratio effect. Over-tip flow leakage is also studied by measuring the static pressure distributions on the blade tip...
Proceedings Papers
Proc. ASME. GT2020, Volume 7B: Heat Transfer, V07BT12A044, September 21–25, 2020
Paper No: GT2020-15101
...FILM COOLING AND HEAT TRANSFER PERFORMANCE OF A FULLY-COOLED TURBINE VANE AT VARIED DENSITY RATIOS AND MASS FLOW RATIOS Chun-yi Yao1, Hui-ren Zhu1,2, Cun-liang Liu1,2, Bo-lun Zhang1, Xin-lei Li1 1School of Power and Energy, Northwestern Polytechnical University, Xi an, China 2Shaanxi Key Laboratory...
Proceedings Papers
Proc. ASME. GT2003, Volume 5: Turbo Expo 2003, Parts A and B, 385-394, June 16–19, 2003
Paper No: GT2003-38582
... 05 02 2009 Film cooling performance was studied on a simulated turbine vane model with an objective of determining how much the coolant density ratio affects this performance. Experiments were conducted using coolant density ratios of 1.8 and 1.2. The purpose of the study...
Proceedings Papers
Proc. ASME. GT2005, Volume 3: Turbo Expo 2005, Parts A and B, 677-687, June 6–9, 2005
Paper No: GT2005-68783
.... The facility simulates the film cooling row flow field on the pressure side of a turbine blade. Engine representative non-dimensionals are achieved, providing a faithful model at larger scale. Heating the free stream air and strongly cooling the coolant gives the required density ratio between coolant and free...
Proceedings Papers
Proc. ASME. GT2006, Volume 3: Heat Transfer, Parts A and B, 127-137, May 8–11, 2006
Paper No: GT2006-90166
... flow field on the pressure side of a turbine blade. Engine representative non-dimensionals are achieved, providing a faithful model at larger scale. Heating the free stream air and strongly cooling the coolant gives the required density ratio between coolant and free-stream. The coolant is injected...